All,

    The perigee Contacts were nominal. The inertial maneuver was successful. Both Orbit’s 671 & 672 ATS’s have been uploaded. The SSR was dumped, and all the missing data was redumped.

 

Tasks Accomplished:

Reset FDC Totals

Set Spacecraft Clock

Dumped Orbit 670 Data

Reset Master Timer

CAR# 1434 Orbit 671 ATS Upload

CAR# 1436 Orbit 672 ATS upload

CAR# 1435 Hi Sweep Contact ATS upload

CAR# 1432 Redump Orbit 669 Blocks

CAR# 1437 Redump Orbit 670 Blocks 

 

Results from the Inertial Maneuver:

Q1 0.63343700 ActNor.EstInrToBdy[0]

Q2 -0.54160000 ActNor.EstInrToBdy[1]

Q3 0.26913700 ActNor.EstInrToBdy[2]

Q4 0.48269300 ActNor.EstInrToBdy[3]

     

GPS sec 1417854619 ActNor.EstTime

UTC time 12/10/2024 08:30:05 output

 

MPS Diff 0.756 deg

 

MPS Cmd Vector X -0.17639300

MPS Cmd Vector Y -0.89916800

MPS Cmd Vector Z -0.40047700

 

CSS Angle TLM 1.31656

CSS Sun-Pointing Angle 2.63312

  06 Dec 24 @19:00:00

 

CSS Angle TLM 0.85257

CSS Sun-Pointing Angle 1.70514

  10 Dec 24 @08:30:00

 

Pre-Burn   

Thruster 1 10288 06 Dec 24 @19:00:00

Thruster 2 10032

Thruster 3 12736

Thruster 4 12992

Post-Burn  

Thruster 1 10688 10 Dec 24 @08:30:00

Thruster 2 10384

Thruster 3 13104

Thruster 4 13408

Number of Pulses  

Thruster 1 400

Thruster 2 352

Thruster 3 368

Thruster 4 416

Thruster Pairs 

Thruster 1 & 2 752

Thruster 3 & 4 784

 

 

 

Timothy E.Perry

CRS IBEX OCO-2

Mission Operations

timothy.perry@ngc.com

Office (703) 406-5976

IBEX MOC (703)404-7470

Cell (301) 606-1430