All,

    The perigee contacts were nominal. The inertial maneuver was successful. We were able to redump the missing data from Orbit 666. The orbit 667 SSR Dump took a hit at the end of the dump. We were able to recover the missing data on the following contact. The Orbit 669 ATS was successfully uplinked.

 

Tasks Accomplished:

SSR Dump -> Dump New

Reset FDC Totals

Reset Master Timer

CAR # 1424 Redump Orbit 666 Missing Blocks

CAR # 1425 Orbit 669 ATS Uplink

   IBEX_2024_327_o0669a_v001

CAR #1427 Redump Orbit 667 Missing Blocks

 

Results from the Inertial Maneuver:

Q1 0.74118800 ActNor.EstInrToBdy[0]

Q2 -0.31223000 ActNor.EstInrToBdy[1]

Q3 -0.21993100 ActNor.EstInrToBdy[2]

Q4 0.55207100 ActNor.EstInrToBdy[3]

     

GPS sec 1415463075 ActNor.EstTime

UTC time 11/12/2024 16:11:01 output

 

MPS Diff 0.768 deg

 

MPS Cmd Vector X -0.66444600

MPS Cmd Vector Y -0.68207300

MPS Cmd Vector Z -0.30542900

 

CSS Angle TLM 0.674056

CSS Sun-Pointing Angle 1.348112

  09 Nov 24 @20:30:00

 

CSS Angle TLM 0.181794

CSS Sun-Pointing Angle 0.363588

  12 Nov 24 @17:00:00

 

Pre-Burn   

Thruster 1 8800 09 Nov 24 @20:30:00

Thruster 2 8592

Thruster 3 10592

Thruster 4 10800

Post-Burn  

Thruster 1 8912 12 Nov 24 @17:00:00

Thruster 2 8704

Thruster 3 10736

Thruster 4 10944

Number of Pulses  

Thruster 1 112

Thruster 2 112

Thruster 3 144

Thruster 4 144

Thruster Pairs 

Thruster 1 & 2 224

Thruster 3 & 4 288

 

 

 

Timothy E.Perry

CRS IBEX OCO-2

Mission Operations

timothy.perry@ngc.com

Office (703) 406-5976

IBEX MOC (703)404-7470

Cell (301) 606-1430