All,

   The perigee contacts were nominal. We had a few errors on the SSR dump, we were able to redump the missing data on the second contact. The missing data for orbit 664 was also redumped with zero errors. The Orbit 667 ATS was uplinked, and the inertial maneuver was successful. The star tracker reset time was 17 Oct 24 @00:12:12gmt. 

 

Tasks Accomplished:

SSR Dump -> Dump New

Reset FDC Totals

Reset Master Timer

CAR #1421 Redump Orbit 664 SSR Blocks

CAR #1422 Orbit #667 ATS upload

    IBEX_2024_308_o0667a_v001 98 Cmd

CAR #1423 Redump Orbit 665 SSR Blocks

 

Results from the Inertial Maneuver:

Q1 0.76551100 ActNor.EstInrToBdy[0]

Q2 0.10782700 ActNor.EstInrToBdy[1]

Q3 -0.59730700 ActNor.EstInrToBdy[2]

Q4 0.21352000 ActNor.EstInrToBdy[3]

 

GPS sec 1413873253 ActNor.EstTime

UTC time 10/25/2024 06:33:59 output

 

MPS Diff 0.656 deg

 

MPS Cmd Vector X -0.86690300

MPS Cmd Vector Y -0.45372600

MPS Cmd Vector Z -0.20642600

 

CSS Angle TLM 0.510141

CSS Sun-Pointing Angle 1.020282

  20 Oct 24 @20:00:00

 

CSS Angle TLM 0.817571

CSS Sun-Pointing Angle 1.635142

  25 Oct 24 @02:30:00

 

Pre-Burn   

Thruster 1 7584 20 Oct 24 @20:00:00

Thruster 2 7376

Thruster 3 9104

Thruster 4 9312

Post-Burn  

Thruster 1 7856 25 Oct 24 @02:30:00

Thruster 2 7648

Thruster 3 9408

Thruster 4 9616

Number of Pulses  

Thruster 1 272

Thruster 2 272

Thruster 3 304

Thruster 4 304

Thruster Pairs 

Thruster 1 & 2 544

Thruster 3 & 4 608

 

 

 

Timothy E.Perry

CRS IBEX OCO-2

Mission Operations

timothy.perry@ngc.com

Office (703) 406-5976

IBEX MOC (703)404-7470

Cell (301) 606-1430