All,

The first perigee contact was nominal for command/telemetry and the inertial maneuver was successful.

 

Tasks Accomplished:

  1. Reset master timer
  2. Reset FDC totals
  3. Set SC time
  4. Dump SSR (new)
  5. CAR# 1414 Orbit#663 HGC ATS Upload (875-938)

 

Results from the Inertial Maneuver:

Q1          -0.70390200

Q2          -0.10206800

Q3          0.69855100

Q4          0.07829600

 

GPS sec 1411484521

UTC time              09/27/2024 15:01:47

MPS Diff               0.717

 

MPS Cmd Vector X           -0.99914900

MPS Cmd Vector Y           -0.03337200

MPS Cmd Vector Z           -0.02422300

 

CSS Angle TLM   0.866601           

CSS Sun-Pointing Angle  1.733202           

                                23 Sept 24 @23:30:00

CSS Angle TLM   0.117037           

CSS Sun-Pointing Angle  0.234074           

                                27 Sept 24 @14:00:00

Pre-Burn                            

Thruster 1           6128     23 Sept 24 @23:30:00

Thruster 2           5968    

Thruster 3           6928    

Thruster 4           7088    

Post-Burn                           

Thruster 1           6432     27 Sept 24 @14:00:00

Thruster 2           6272    

Thruster 3           7216    

Thruster 4           7376    

Number of Pulses                            

Thruster 1           304       

Thruster 2           304       

Thruster 3           288       

Thruster 4           288       

Thruster Pairs                   

Thruster 1 & 2   608       

Thruster 3 & 4   576       

 

 

Best Regards,

 

Sheral Wesley  |  Sr Principal Engineer, Satellite Systems

Northrop Grumman Corporation  |  Space Systems

O: 703-406-5641  |  C: 202-236-0802  |  sheral.wesley@ngc.com

 

From: Perry, Timothy E [US] (SP) <Timothy.Perry@ngc.com>
Sent: Monday, September 23, 2024 8:09 PM
To: bhautama@gmail.com; carol.weaver@unh.edu; Cavallo, John A [US] (SP) <John.Cavallo@ngc.com>; Chubin, Eric [US] (SP) <Eric.Chubin@ngc.com>; Coca Gonzales, Andrea [US] (SP) <Andrea.CocaGonzales@ngc.com>; Fleming, Ed [US] (SP) <Ed.Fleming@ngc.com>; ADS-IBEX@l3harris.com; ibexops@gmail.com; IBEXOPS@gmail.com; isocops@lists.sr.unh.edu; kwfairchild@gmail.com; Ken.Fairchild@unh.edu; Leonard, Ben [US] (SP) <Benjamin.Leonard@ngc.com>; angoldconsulting@earthlink.net; nangold@princeton.edu; Perry, Timothy E [US] (SP) <Timothy.Perry@ngc.com>; Reed, Cheryl L [US] (SP) <Cheryl.Reed@ngc.com>; Tyler, Ryan S [US] (SP) <Ryan.Tyler@ngc.com>; Wesley, Sheral R [US] (SP) <Sheral.Wesley@ngc.com>; Wynn, Reese [US] (SP) <Reese.Wynn@ngc.com>; ezirnstein@swri.edu
Subject: IBEX Goat Herder for 23 Sept 2024

 

All,

   The apogee contact was nominal. The inertial maneuver was successful.

 

Tasks Accomplished:

Reset FDC totals

 

Results from the Inertial Maneuver:

Q1 0.69799500 ActNor.EstInrToBdy[0]

Q2 -0.04554130 ActNor.EstInrToBdy[1]

Q3 -0.71443000 ActNor.EstInrToBdy[2]

Q4 0.01786840 ActNor.EstInrToBdy[3]

     

GPS sec 1411169500 ActNor.EstTime

UTC time 09/23/2024 23:31:26 output

 

MPS Diff 0.844 deg

 

MPS Cmd Vector X -0.99918000

MPS Cmd Vector Y 0.03992200

MPS Cmd Vector Z 0.00673700

 

CSS Angle TLM 1.30409

CSS Sun-Pointing Angle 2.60818

  18 Sept 24 @07:00:00

 

CSS Angle TLM 0.866601

CSS Sun-Pointing Angle 1.733202

  23 Sept 24 @23:30:00

 

Pre-Burn   

Thruster 1 6000 18 Sept 24 @07:00:00

Thruster 2 5840

Thruster 3 6784

Thruster 4 6944

Post-Burn  

Thruster 1 6128 23 Sept 24 @23:30:00

Thruster 2 5968

Thruster 3 6928

Thruster 4 7088

Number of Pulses 

Thruster 1 128

Thruster 2 128

Thruster 3 144

Thruster 4 144

Thruster Pairs 

Thruster 1 & 2 256

Thruster 3 & 4 288

 

 

 

 

Timothy E.Perry

CRS IBEX OCO-2

Mission Operations

timothy.perry@ngc.com

Office (703) 406-5976

Cell (301) 606-1430