All,

    The apogee contact was nominal. The inertial maneuver was successful. We were able to switch over to maestro string3 and checkout the system. Initial checks look good.

 

 

Results from the inertial Maneuver:

Q1 -0.65458300 ActNor.EstInrToBdy[0]

Q2 -0.02618350 ActNor.EstInrToBdy[1]

Q3 0.70427900 ActNor.EstInrToBdy[2]

Q4 0.27354500 ActNor.EstInrToBdy[3]

     

GPS sec 1409527910 ActNor.EstTime

UTC time 09/04/2024 23:31:36 output

 

MPS Diff 0.772 deg

 

MPS Cmd Vector X -0.93846700

MPS Cmd Vector Y 0.32061400

MPS Cmd Vector Z 0.12839800

 

CSS Angle TLM 0.338041

CSS Sun-Pointing Angle 0.676082

  30 Aug 24 @21:00:00

 

CSS Angle TLM 0.449805

CSS Sun-Pointing Angle 0.89961

  04 Sept 24 @23:30:00

 

Pre-Burn   

Thruster 1 4944 30 Aug 24 @21:00:00

Thruster 2 4848

Thruster 3 5184

Thruster 4 5280

Post-Burn  

Thruster 1 5216 04 Sept 24 @23:30:00

Thruster 2 5120

Thruster 3 5472

Thruster 4 5568

Number of Pulses 

Thruster 1 272

Thruster 2 272

Thruster 3 288

Thruster 4 288

Thruster Pairs 

Thruster 1 & 2 544

Thruster 3 & 4 576

 

 

 

Timothy E.Perry

CRS IBEX OCO-2

Mission Operations

timothy.perry@ngc.com

Office (703) 406-5976

IBEX MOC (703)404-7470

Cell (301) 606-1430