All,

    The spacecraft is nominal. The perigee inertial maneuver was successful. Both orbit’s 660 and 661 ats was uplinked. The SSR was dumped with zero errors. The second contact was used for monitoring SOH. The AGC was low and not a good pass for commanding.

 

 

Tasks Accomplished:

SSR Dump -> Dump_New

Reset Master Timer

Reset FDC Totals

CAR #1411 Orbit# 660 ATS Upload

   IBEX_2024_244_o0660a_V002 98 cmds

CAR  #1409 Orbit# 661 ATS Upload

   IBEX_2024_253_o0661a_V001 96 cmds

 

Results from the Inertial Maneuver:

Q1 0.30170100 ActNor.EstInrToBdy[0]

Q2 -0.56919700 ActNor.EstInrToBdy[1]

Q3 -0.59503500 ActNor.EstInrToBdy[2]

Q4 0.48054700 ActNor.EstInrToBdy[3]

     

GPS sec 1409087092 ActNor.EstTime

UTC time 08/30/2024 21:04:38 output

 

MPS Diff 0.733 deg

 

MPS Cmd Vector X -0.90894100

MPS Cmd Vector Y 0.38601000

MPS Cmd Vector Z 0.15755500

 

CSS Angle TLM 0.349246

CSS Sun-Pointing Angle 0.698492

  25 Aug 24 @23:30:00

 

CSS Angle TLM 0.338041

CSS Sun-Pointing Angle 0.676082

  30 Aug 24 @21:00:00

 

Pre-Burn   

Thruster 1 4672 25 Aug 24 @23:30:00

Thruster 2 4576

Thruster 3 4880

Thruster 4 4976

Post-Burn  

Thruster 1 4944 30 Aug 24 @21:00:00

Thruster 2 4848

Thruster 3 5184

Thruster 4 5280

Number of Pulses 

Thruster 1 272

Thruster 2 272

Thruster 3 304

Thruster 4 304

Thruster Pairs 

Thruster 1 & 2 544

Thruster 3 & 4 608

 

 

 

Timothy E.Perry

CRS IBEX OCO-2

Mission Operations

timothy.perry@ngc.com

Office (703) 406-5976

IBEX MOC (703)404-7470

Cell (301) 606-1430