Good morning team,
The ground station was having some issues this morning and we were unable to command during this contact. We had a star tracker reset before the pass and the errors have not yet been cleared due to our inability
to command. Tim has sent out a request to schedule a blind acq for DOY 150 at 12:00z to clear the reset errors. The inertial maneuver was successful.
Results from the inertial maneuver:
Q1 -0.52751700
Q2 -0.20507500
Q3 -0.61784800
Q4 0.54583300
GPS sec 140093331
UTC time 06/14/1984 10:48:37
MPS Diff 0.592
MPS Cmd Vector X 0.42454600
MPS Cmd Vector Y 0.83455000
MPS Cmd Vector Z 0.35112300
CSS Angle TLM 0.0667314
CSS Sun-Pointing Angle 0.1334628
24 May 24 @22:00:00
CSS Angle TLM 0.222056
CSS Sun-Pointing Angle 0.444112
28 May 24 @12:00:00
Pre-Burn
Thruster 1 25264 24 May 24 @13:00:00
Thruster 2 24544
Thruster 3 33040
Thruster 4 33760
Post-Burn
Thruster 1 25520 28 May 24 @12:00:00
Thruster 2 24800
Thruster 3 33328
Thruster 4 34048
Number of Pulses
Thruster 1 256
Thruster 2 256
Thruster 3 288
Thruster 4 288
Thruster Pairs
Thruster 1 & 2 512
Thruster 3 & 4 576
Best,
Andrea Coca Gonzales | Associate
Engineer Satellite Systems | MEV | ICESat-2 | TESS | IBEX
Northrop Grumman Corporation | Space Systems
C: 703-582-8233 |
Andrea.CocaGonzales@ngc.com