Good morning team,
The perigee contacts were nominal, and the inertial maneuver was successful. We performed the following, dump SSR (VCid2), dump missing SSR blocks (CAR#1392)
and reset master timer. Both contacts were done on maestro IBEX-1.
Tasks Accomplished:
Reset Master Timer
Reset FDC Totals
FC Back orbit dump (VCid1)
SSR Dump New (VCid2)
SSR Dump Nblocks (CAR#1392)
CAR #1391 Orbit 649 ATS upload
IBEX_2024_144_o0649a_v001 - 101 commands
Results from the inertial maneuver:
Q1 -0.47333300
Q2 0.34489400
Q3 -0.05921270
Q4 0.80839200
GPS sec 1399813686
UTC time 05/15/2024 13:07:52
MPS Diff 0.521
MPS Cmd Vector X 0.61459100
MPS Cmd Vector Y 0.72729600
MPS Cmd Vector Z 0.30547900
CSS Angle TLM 0.351102
CSS Sun-Pointing Angle 0.702204
10 May 24 @13:00:00
CSS Angle TLM 0.3743
CSS Sun-Pointing Angle 0.7486
14 May 24 @22:00:00
Pre-Burn
Thruster 1 24448 10 May 24 @13:00:00
Thruster 2 23760
Thruster 3 32176
Thruster 4 32864
Post-Burn
Thruster 1 24736 14 May 24 @22:00:00
Thruster 2 24016
Thruster 3 32480
Thruster 4 33200
Number of Pulses
Thruster 1 288
Thruster 2 256
Thruster 3 304
Thruster 4 336
Thruster Pairs
Thruster 1 & 2 544
Thruster 3 & 4 640
Kind regards,
Andrea Coca Gonzales | Associate
Engineer Satellite Systems | MEV | ICESat-2 | TESS | IBEX
Northrop Grumman Corporation | Space Systems
C: 703-582-8233 |
Andrea.CocaGonzales@ngc.com