Good morning team,
The perigee contacts were nominal, and the inertial maneuver was successful. We performed the following, dump SSR( VCid2), re-dump missing SSR blocks, and
reset master timer.
Tasks Accomplished:
Reset Master Timer
Reset FDC Totals
SSR Dump -> Dump New
SSR Dump -> NBlocks (CAR #1389)
CAR #1387 Orbit 645 ATS upload
IBEX_2024_126_o0647a_v001 98 commands
Results from the inertial maneuver:
Q1 -0.54954600
Q2 -0.29253100
Q3 -0.78078100
Q4 0.05297460
GPS sec 1398239249
UTC time
04/27/2024 07:47:15
MPS Diff
0.707
MPS Cmd Vector X
0.82345600
MPS Cmd Vector Y
0.524094000
MPS Cmd Vector Z
0.217360000
CSS Angle TLM 0.3456
CSS Sun-Pointing Angle 0.6912
22 Apr 24 @13:00:00
CSS Angle TLM 0.137056
CSS Sun-Pointing Angle 0.274112
26 Apr 24 @19:00:00
Pre-Burn
Thruster 1 23344 22 Apr 24 @13:00:00
Thruster 2 22656
Thruster 3 30960
Thruster 4 31648
Post-Burn
Thruster 1 23632 26 Apr 24 @19:00:00
Thruster 2 22944
Thruster 3 31264
Thruster 4 31952
Number of Pulses
Thruster 1 288
Thruster 2 288
Thruster 3 304
Thruster 4 304
Thruster Pairs
Thruster 1 & 2 576
Thruster 3 & 4 608
Andrea Coca Gonzales | Associate
Engineer Satellite Systems | MEV | ICESat-2 | TESS
Northrop Grumman Corporation | Space Systems
C: 703-582-8233 |
Andrea.CocaGonzales@ngc.com