All,

    The perigee contacts were nominal. The inertial maneuver was successful. During the first contact we uplinked the Hi Normal Sweep table. The ATS for orbit 644 was uplinked and the SSR was dumped for orbit #642.

 

Tasks Accomplished:

Reset FDC Totals

Reset Master Timer

SSR dump -> dump New

CAR #1335 2024 ISN Season & Hi Background Test Sweep Table upload

  Pass#6 Upload Hi Normal Sweep Table

CAR #1383 Orbit #644 ATS Upload

   IBEX_2024_099_o0644a_v001 103 commands

 

Results from Inertial Maneuver:

Q1 0.52846000 ActNor.EstInrToBdy[0]

Q2 0.43984300 ActNor.EstInrToBdy[1]

Q3 0.61134700 ActNor.EstInrToBdy[2]

Q4 0.39181900 ActNor.EstInrToBdy[3]

     

GPS sec 1395871235 ActNor.EstTime

UTC time 03/30/2024 22:00:21 output

 

MPS Diff 0.565 deg

 

MPS Cmd Vector X 0.99079000

MPS Cmd Vector Y 0.127538000

MPS Cmd Vector Z 0.045485000

 

CSS Angle TLM 0.831101

CSS Sun-Pointing Angle 1.662202

  25 Mar 24 @16:30:00

 

CSS Angle TLM 0.273398

CSS Sun-Pointing Angle 0.546796

  30 Mar 24 @22:00:00

 

Pre-Burn   

Thruster 1 21696 25 Mar 24 @16:30:00

Thruster 2 21040

Thruster 3 29168

Thruster 4 29824

Post-Burn  

Thruster 1 21968 30 Mar 24 @22:00:00

Thruster 2 21312

Thruster 3 29488

Thruster 4 30144

Number of Pulses  

Thruster 1 272

Thruster 2 272

Thruster 3 320

Thruster 4 320

Thruster Pairs 

Thruster 1 & 2 544

 

 

Timothy E.Perry

CRS IBEX OCO-2

Mission Operations

timothy.perry@ngc.com

Office (703) 406-5976

IBEX MOC (703)404-7470

Cell (301) 606-1430