All,

    The perigee contacts were nominal. The inertial maneuver was successful. The Orbit 463 ats was uplinked. The Hi background sweep table was successfully uplinked.

 

Tasks Accomplished:

SSR Dump -> Dump New

CAR # 1335 2024 ISN Season and Hi Background test sweep table uploads

Pass # 5 Upload Hi Background Sweep table

CAR # 1382 Orbit # 643 ATS upload

   IBEX_2024)090_o0643a_v001 101 commands

Reset FDC Totals

Reset Master Timer

 

Results from the Inertial Maneuver:

Q1 0.47996900 ActNor.EstInrToBdy[0]

Q2 0.51852200 ActNor.EstInrToBdy[1]

Q3 0.47968800 ActNor.EstInrToBdy[2]

Q4 0.52025400 ActNor.EstInrToBdy[3]

     

GPS sec 1395076040 ActNor.EstTime

UTC time 03/21/2024 17:07:06 output

 

MPS Diff 0.818 deg

 

MPS Cmd Vector X 0.99993000

MPS Cmd Vector Y 0.010454000

MPS Cmd Vector Z -0.005515000

 

CSS Angle TLM 0.974179

CSS Sun-Pointing Angle 1.948358

  16 Mar 24 @13:00:00

 

CSS Angle TLM 0.773796

CSS Sun-Pointing Angle 1.547592

  21 Mar 24 @17:00:00

 

Pre-Burn   

Thruster 1 21344 16 Mar 24 @13:00:00

Thruster 2 20688

Thruster 3 28752

Thruster 4 29408

Post-Burn  

Thruster 1 21520 21 Mar 24 @17:00:00

Thruster 2 20864

Thruster 3 28944

Thruster 4 29600

Number of Pulses  

Thruster 1 176

Thruster 2 176

Thruster 3 192

Thruster 4 192

Thruster Pairs 

Thruster 1 & 2 352

Thruster 3 & 4 384

 

 

 

Timothy E.Perry

CRS IBEX OCO-2

Mission Operations

timothy.perry@ngc.com

Office (703) 406-5976

IBEX MOC (703)404-7470

Cell (301) 606-1430