All,

   The perigee contacts were nominal. The inertial maneuver was successful. The SSR was dumped with 0 errors AND THE HI Gain Curve ATS was uplinked.

 

Tasks Accomplished:

Reset FDC Totals

SSR Dump -> Dump New

Reset Master Timer

CAR#1372 Hi Gain Curve ATS upload

   IBEX_2024_063_o0640a_v001_HGC 64 Commands

 

Results from the Inertial Maneuver:

Q1 -0.60464400 ActNor.EstInrToBdy[0]

Q2 0.43695300 ActNor.EstInrToBdy[1]

Q3 -0.62173400 ActNor.EstInrToBdy[2]

Q4 0.23858600 ActNor.EstInrToBdy[3]

     

GPS sec 1393481309 ActNor.EstTime

UTC time 03/03/2024 06:08:15 output

 

MPS Diff 0.441 deg

 

MPS Cmd Vector X 0.95997300

MPS Cmd Vector Y -0.252847000

MPS Cmd Vector Z -0.120501000

 

CSS Angle TLM 1.36702

CSS Sun-Pointing Angle 2.73404

  27 Feb 24 @15:00:00

 

CSS Angle TLM 0.86818

CSS Sun-Pointing Angle 1.73636

  03 Mar 24 @06:00:00

 

Pre-Burn   

Thruster 1 20144 27 Feb 24 @15:00:00

Thruster 2 19536

Thruster 3 27488

Thruster 4 28096

Post-Burn  

Thruster 1 20512 03 Mar 24 @06:00:00

Thruster 2 19856

Thruster 3 27856

Thruster 4 28512

Number of Pulses  

Thruster 1 368

Thruster 2 320

Thruster 3 368

Thruster 4 416

Thruster Pairs 

Thruster 1 & 2 688

Thruster 3 & 4 784

 

 

 

Timothy E.Perry

CRS IBEX OCO-2

Mission Operations

timothy.perry@ngc.com

Office (703) 406-5976

IBEX MOC (703)404-7470

Cell (301) 606-1430