All,

    The spacecraft is nominal. The inertial maneuver was successful. We commanded the Hi sweep table back to normal sweep. The ATS for Orbit 634 has been uplinked and the SSR data for orbit 632 has been downlinked.

 

Tasks Accomplished:

CAR# 1335 – ISN Season and Hi background test Sweep table uplink

  Pass #3 Upload Hi Normal Sweep Table (completed)

CAR# 1363 – Orbit # 634 ATS Upload

   IBEX_2024_007_o0634a_v001 96 Commands

Set Spacecraft Clock

Reser FDC Totals

SSR Dump -> Dump New

 

 

Results from the Inertial Maneuver:

Q1 0.09790130 ActNor.EstInrToBdy[0]

Q2 0.82868400 ActNor.EstInrToBdy[1]

Q3 -0.53067400 ActNor.EstInrToBdy[2]

Q4 0.14860500 ActNor.EstInrToBdy[3]

     

GPS sec 1387927852 ActNor.EstTime

UTC time 12/29/2023 23:30:38 output

 

MPS Diff 0.720 deg

 

MPS Cmd Vector X 0.14807800

MPS Cmd Vector Y -0.903368000

MPS Cmd Vector Z -0.402491000

 

CSS Angle TLM 0.91564

CSS Sun-Pointing Angle 1.83128

  24 Dec 23 @16:00:00

 

CSS Angle TLM 1.31

CSS Sun-Pointing Angle 2.62

  29 Dec 23 @23:30:00

 

Pre-Burn   

Thruster 1 16896 24 Dec 23 @16:00:00

Thruster 2 16384

Thruster 3 22368

Thruster 4 22880

Post-Burn  

Thruster 1 17200 29 Dec 23 @23:30:00

Thruster 2 16688

Thruster 3 22672

Thruster 4 23184

Number of Pulses  

Thruster 1 304

Thruster 2 304

Thruster 3 304

Thruster 4 304

Thruster Pairs 

Thruster 1 & 2 608

Thruster 3 & 4 608

 

 

 

Timothy E.Perry

CRS IBEX OCO-2

Mission Operations

timothy.perry@ngc.com

Office (703) 406-5976

IBEX MOC (703)404-7470

Cell (301) 606-1430