All,

    The perigee contacts were nominal. The inertial maneuver was successful. We updated the Hi sweep table from normal to background. The SSR was dumped and the orbit 633 ATS was uplinked.

 

Tasks Accomplished:

SSR Dump -> Dump New

Reset FDC Totals

Reset Master Timer

CAR # 1335 - 2024 ISN Season and Hi Background sweep test

Completed Pass #2 – Upload Hi Background table

CAR #1362 – Orbit #633 ATS Upload

   IBEX_2023_363_o0633a_v001 98 commands

 

Results from the Inertial maneuver:

Q1 0.80863500 ActNor.EstInrToBdy[0]

Q2 0.20832400 ActNor.EstInrToBdy[1]

Q3 -0.14915900 ActNor.EstInrToBdy[2]

Q4 0.52958700 ActNor.EstInrToBdy[3]

     

GPS sec 1387080001 ActNor.EstTime

UTC time 12/20/2023 03:59:47 output

 

MPS Diff 0.794 deg

 

MPS Cmd Vector X -0.01682000

MPS Cmd Vector Y -0.913355000

MPS Cmd Vector Z -0.406816000

 

CSS Angle TLM 1.07265

CSS Sun-Pointing Angle 2.1453

  15 Dec 23 @21:00:00

 

CSS Angle TLM 0.762589

CSS Sun-Pointing Angle 1.525178

  20 Dec 23 @04:00:00

 

Pre-Burn   

Thruster 1 16288 15 Dec 23 @21:00:00

Thruster 2 15776

Thruster 3 21696

Thruster 4 22208

Post-Burn  

Thruster 1 16624 20 Dec 23 @04:00:00

Thruster 2 16112

Thruster 3 22064

Thruster 4 22576

Number of Pulses  

Thruster 1 336

Thruster 2 336

Thruster 3 368

Thruster 4 368

Thruster Pairs 

Thruster 1 & 2 672

Thruster 3 & 4 736

 

 

 

Timothy E.Perry

CRS IBEX OCO-2

Mission Operations

timothy.perry@ngc.com

Office (703) 406-5976

Cell (301) 606-1430