All,

   The perigee contacts were nominal. The inertial maneuver was successful. We dumped the SSR data for orbit 630. We were able to redump missing data from both orbits 629 & 630. The orbit 632 ATS was uplinked.

 

Tasks Accomplished:

CAR #1359 Redump missing orbit 629 blocks

CAR #1360 Orbit 632 ATS upload

    IBEX_2023_354_o0632a_v001 108 cmds

CAR #1361 Redump missing orbit 630 blocks

Set Spacecraft clock

Dumped Flight Computer Back Orbit Data

Reset FDC Totals

Reset Master Timer

 

Results from the Inertial Maneuver:

Q1 0.25915800 ActNor.EstInrToBdy[0]

Q2 -0.79274700 ActNor.EstInrToBdy[1]

Q3 0.47983600 ActNor.EstInrToBdy[2]

Q4 0.27229700 ActNor.EstInrToBdy[3]

     

GPS sec 1386302522 ActNor.EstTime

UTC time 12/11/2023 04:01:48 output

 

MPS Diff 0.652 deg

 

MPS Cmd Vector X -0.17728000

MPS Cmd Vector Y -0.898951000

MPS Cmd Vector Z -0.400573000

 

CSS Angle TLM 1.24678

CSS Sun-Pointing Angle 2.49356

  06 Dec 23 @23:30:00

 

CSS Angle TLM 1.14261

CSS Sun-Pointing Angle 2.28522

  11 Dec 23 @04:00:00

 

Pre-Burn   

Thruster 1 15808 06 Dec 23 @23:30:00

Thruster 2 15344

Thruster 3 20960

Thruster 4 21424

Post-Burn  

Thruster 1 16144 11 Dec 23 @04:00:00

Thruster 2 15680

Thruster 3 21296

Thruster 4 21760

Number of Pulses  

Thruster 1 336

Thruster 2 336

Thruster 3 336

Thruster 4 336

Thruster Pairs 

Thruster 1 & 2 672

Thruster 3 & 4 672

 

 

 

Timothy E.Perry

CRS IBEX OCO-2

Mission Operations

timothy.perry@ngc.com

Office (703) 406-5976

Cell (301) 606-1430