All,

   The perigee contacts were nominal. The inertial maneuver was successful. We were able to achieve 320k downlink, so we were able to dump all the SSR data for orbits 619 & 620.  The Lo sweep table was changed from magnetotail sweep to normal sweep. The ATS for orbit 622 was uplinked.

 

Tasks Accomplished:

Reset FDC Totals

Reset the Master Timer

SSR Dump -> Dump New

CAR #1301 IBEX Background test and Lo 2023 Magnetotail season

   Pass #3 Upload Lo Normal Sweep Table

CAR #1339 Orbit 622 ATS upload

   IBEX_2023_264_o0622a_v001 91 commands

 

Results from the Inertial Maneuver:

Q1 0.14480300 ActNor.EstInrToBdy[0]

Q2 -0.65580700 ActNor.EstInrToBdy[1]

Q3 -0.31847900 ActNor.EstInrToBdy[2]

Q4 0.66897000 ActNor.EstInrToBdy[3]

     

GPS sec 1378569657 ActNor.EstTime

UTC time 09/12/2023 16:00:43 output

 

MPS Diff 0.773 deg

 

MPS Cmd Vector X -0.97186800

MPS Cmd Vector Y 0.219519000

MPS Cmd Vector Z 0.085347000

 

CSS Angle TLM 0.224684

CSS Sun-Pointing Angle 0.449368

  07 Sept 23@07:00:00

 

CSS Angle TLM 0.484164

CSS Sun-Pointing Angle 0.968328

  12 Sept 23@16:00:00

 

Pre-Burn   

Thruster 1 11280 07 Sept 23@07:00:00

Thruster 2 11008

Thruster 3 13488

Thruster 4 13760

 

Post-Burn  

Thruster 1 11552 12 Sept 23@16:00:00

Thruster 2 11280

Thruster 3 13792

Thruster 4 14064

Number of Pulses  

Thruster 1 272

Thruster 2 272

Thruster 3 304

Thruster 4 304

Thruster Pairs 

Thruster 1 & 2 544

Thruster 3 & 4 608

 

 

 

Timothy E.Perry

CRS IBEX OCO-2

Mission Operations

timothy.perry@ngc.com

Office (703) 406-5976

Cell (301) 606-1430