All,

   The perigee contacts were nominal. The inertial maneuver was successful. The star tracker was at 74% valid at the time of the maneuver. We dumped the SSR during both contacts. The master timer was reset. During the contacts we executed commands to check some star tracker parameters.

 

Tasks accomplished:

CAR # 1311 Orbit #607 ATS upload

   IBEX_2023_127_o0607a_v001 101 CMDS

SSR Dump -> dump new 2ea

Reset Master timer

Ops_ACS_Tracker_Params_Dump.scr

 

Results from the Inertial Maneuver:

Q1 0.35134800 ActNor.EstInrToBdy[0]

Q2 0.51318400 ActNor.EstInrToBdy[1]

Q3 0.72062800 ActNor.EstInrToBdy[2]

Q4 0.30641800 ActNor.EstInrToBdy[3]

     

GPS sec 1366714919 ActNor.EstTime

UTC time 04/28/2023 11:01:45 output

 

MPS Diff 0.471 deg

 

MPS Cmd Vector X 0.820950000

MPS Cmd Vector Y 0.527405000

MPS Cmd Vector Z 0.218825000

 

CSS Angle TLM 0.990908

CSS Sun-Pointing Angle 1.981816

  23 Apr 23@15:00:00

 

CSS Angle TLM 0.376285

CSS Sun-Pointing Angle 0.75257

  28 Apr 23@11:00:00

 

Pre-Burn   

Thruster 1 3120 23 Apr 23@15:00:00

Thruster 2 3040

Thruster 3 4480

Thruster 4 4560

Post-Burn  

Thruster 1 3408 28 Apr 23@11:00:00

Thruster 2 3328

Thruster 3 4832

Thruster 4 4912

Number of Pulses  

Thruster 1 288

Thruster 2 288

Thruster 3 352

Thruster 4 352

Thruster Pairs 

Thruster 1 & 2 576

Thruster 3 & 4 704

 

 

 

Timothy E.Perry

CRS IBEX OCO-2

Mission Operations

timothy.perry@ngc.com

Office (703) 406-5976

Cell (301) 606-1430

 

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