Let's discuss on tomorrow's ops call.

Nigel
ADS-IBEX@L3Harris.com
April 3, 2023 at 09:10

Hi all,

 

I can redo the predicts with the updated maneuvers. Nigel, to clarify, are you wanting an updating star tracker outage report?

 

I will just need to know whether the perigee inertial maneuver was executed or not – which sounds like the same question that was stated below regarding whether we had any pulses for it.

 

Thanks!

Kayton

 

Kayton Lane

Astrodynamics Engineer

Space & airborne systems / L3HARRIS TECHNOLOGIES

w +1 321 729 1809

m +1 218 431 0586

L3Harris.com / Kayton.Lane@L3Harris.com

Palm Bay, FL 32905 / USA

 

From: Nigel Angold <nangold@princeton.edu>
Sent: Monday, April 3, 2023 7:59 AM
To: Perry, Timothy E [US] (SP) <Timothy.Perry@ngc.com>
Cc: bhautama@gmail.com; carol.weaver@unh.edu; Chubin, Eric [US] (SP) <Eric.Chubin@ngc.com>; SM[SSTC] - ADS-IBEX <ADS-IBEX@L3Harris.com>; IBEXOPS@gmail.com; isocops@lists.sr.unh.edu; fair-play@comcast.net; kwfairchild@gmail.com; ken.fairchild@unh.edu; Leonard, Benjamin Y [US] (SP) <Benjamin.Leonard@ngc.com>; angoldconsulting@earthlink.net; Tyler, Ryan S [US] (SP) <Ryan.Tyler@ngc.com>; Wesley, Sheral R [US] (SP) <Sheral.Wesley@ngc.com>; Wynn, Reese [US] (SP) <Reese.Wynn@ngc.com>
Subject: [EXTERNAL] Re: IBEX Goat Herder for 3 April 2023

 

WARNING: Email originated from an EXTERNAL source. Do NOT click links, open attachments or reply unless you recognize sender and know the content is safe.

Thanks, Tim and Ken for working this.

 

Is there any chance that we were in a partial outage because of the failed maneuver followed by the Sun pointing maneuver instead of the inertial? I’m not sure if that would explain the percent valid bouncing around  like that. But it’s odd that the value was back up to a solid 78-80% last contact.

 

Did we have any pulses for the failed maneuver?

 

Would FD running the predicts with the actual attitudes be useful/possible?

 

Thanks,

Nigel

Sent from my iPhone




 
 

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Nigel Angold
April 3, 2023 at 07:59
Thanks, Tim and Ken for working this.

Is there any chance that we were in a partial outage because of the failed maneuver followed by the Sun pointing maneuver instead of the inertial? I’m not sure if that would explain the percent valid bouncing around  like that. But it’s odd that the value was back up to a solid 78-80% last contact.

Did we have any pulses for the failed maneuver?

Would FD running the predicts with the actual attitudes be useful/possible?

Thanks,
Nigel

Sent from my iPhone

Perry, Timothy E [US] (SP)
April 3, 2023 at 05:13

All,

   The contact was successful. We were able to delete all the timed commands and uplink a new Orbit 603 ATS version 2. On previous contacts we were seeing the star tracker percent valid value jump around from 0 – 80. That was what caused the spacecraft to go into contingence mode during the perigee inertial maneuver. This contact the star tracker percent valid was stable between 78 & 80.

 

Tasks Accomplished:

Ops Procedure OP924-31423 Delete timed commands

CAR # 1307 Orbit 603 Version 2 ATS uplink

Reset FDC Totals

 

 

 

Timothy E.Perry

CRS IBEX OCO-2

Mission Operations

timothy.perry@ngc.com

Office (703) 406-5976

Cell (301) 606-1430