All,
The spacecraft is nominal and the inertial maneuver was successful. We had another ACE reset on 01/24/23 @21:14:00 GMT. The Spin Pulse Protect was set to enabled, the Kalman filter input was set to GND_CMD. I executed CAR #1004 ACE Reset Recovery and
CAR # 1289 Disable Spin Pulse protect. The spin pulse protect was set back to disabled and re-enabled the ACE Fault detection and correction back to enabled. The perigee maneuver commands took care of the Kalman filter input and set it back to STA_PCT_Valid.
The static Z rate and the estimator rate was nominal. Razor number I100 715 - ACE Reset 24 Jan 23 has been assigned.
We also were able to dump the SSR, reset the master timer and reset the FDC totals. The Orbit 597 ATS was uplinked on the first pass.
Tasks Accomplished:
CAR #1004 ACE Reset Recovery
CAR # 1289 Disable Spin Pulse protect
CAR # 1291 Orbit #597 ATS upload
IBEX_2023_036_o0597a_v001 98 cmds
Reset FDC Totals
Set the Spacecraft Clock
Results from the Inertial Maneuver:
Q1 0.73773100 ActNor.EstInrToBdy[0]
Q2 -0.33512100 ActNor.EstInrToBdy[1]
Q3 0.52965800 ActNor.EstInrToBdy[2]
Q4 0.25081700 ActNor.EstInrToBdy[3]
GPS sec 1358834520 ActNor.EstTime
UTC time
01/27/2023 06:01:46 output
MPS Diff
0.685 deg
MPS Cmd Vector X 0.616646000
MPS Cmd Vector Y -0.718234000
MPS Cmd Vector Z -0.322315000
CSS Angle TLM 0.29072
CSS Sun-Pointing Angle 0.58144
24 Jan
23@18:00:00
CSS Angle TLM 0.629318
CSS Sun-Pointing Angle 1.258636
27 Jan
23@06:00:00
Pre-Burn
Thruster 1 0 24 Jan 23@21:15:00
Thruster 2 0
Thruster 3 0
Thruster 4 0
Post-Burn
Thruster 1 352 27 Jan 23@06:00:00
Thruster 2 352
Thruster 3 384
Thruster 4 384
Number of Pulses
Thruster 1 352
Thruster 2 352
Thruster 3 384
Thruster 4 384
Thruster Pairs
Thruster 1 & 2 704
Thruster 3 & 4 768