All,
The perigee contacts were nominal and the inertial maneuver was successful. We were able to set the spacecraft clock. We reset the master timer and reset FDC totals. The ATS for orbit #576 was uplinked.
Tasks Accomplished:
Reset FDC Totals
SSR Dump -> Dump New
Set Spacecraft Time
Reset Master Timer
CAR #1245 Orbit #576 ATS uplink
IBEX_2022_209_o0576a_v002 100 Cmds
Results from the Inertial Maneuver:
Q1 0.07040360 ActNor.EstInrToBdy[0]
Q2 -0.55846200 ActNor.EstInrToBdy[1]
Q3 -0.78356300 ActNor.EstInrToBdy[2]
Q4 0.26303600 ActNor.EstInrToBdy[3]
GPS sec 1342295384 ActNor.EstTime
UTC time
07/19/2022 19:49:30 output
MPS Diff
0.810 deg
MPS Cmd Vector X -0.411305000
MPS Cmd Vector Y 0.839839000
MPS Cmd Vector Z 0.354258000
CSS Angle TLM 0.326259
CSS Sun-Pointing Angle 0.652518
15 July 22 @10:00:00
CSS Angle TLM 0.27052
CSS Sun-Pointing Angle 0.54104
19 July 22 @19:30:00
Pre-Burn
Thruster 1 2224 15 July 22 @10:00:00
Thruster 2 2160
Thruster 3 2704
Thruster 4 2768
Post-Burn
Thruster 1 2512 19 July 22 @19:30:00
Thruster 2 2448
Thruster 3 2992
Thruster 4 3056
Number of Pulses
Thruster 1 288
Thruster 2 288
Thruster 3 288
Thruster 4 288
Thruster Pairs
Thruster 1 & 2 576
Thruster 3 & 4 576