All,
The spacecraft is nominal. The inertial maneuver was successful. The spacecraft clock was set and the master timer was reset. The SSR was dumped. The Orbit 558 ATS was uplinked.
Tasks Accomplished:
Set Spacecraft Clock
Reset FDC Totals
Reset 18 day timer
SSR Dump -> Dump New
CAR # 1225 Orbit #558 ATS upload
IBEX_2022_047_o0558a_v001 93 cmds
Inertial Maneuver results:
Q1 0.72579000 ActNor.EstInrToBdy[0]
Q2 0.32231100 ActNor.EstInrToBdy[1]
Q3 0.27962900 ActNor.EstInrToBdy[2]
Q4 0.53958500 ActNor.EstInrToBdy[3]
GPS sec 1328225395 ActNor.EstTime
UTC time
02/06/2022 23:29:41 output
MPS Diff
0.587 deg
MPS Cmd Vector X 0.752686000
MPS Cmd Vector Y -0.599980000
MPS Cmd Vector Z -0.271088000
CSS Angle TLM 0.819483
CSS Sun-Pointing Angle 1.638966
03 Feb 22 @ 18:00:00
CSS Angle TLM 0.823057
CSS Sun-Pointing Angle 1.646114
06 Feb 22 @ 23:30:00
Pre-Burn
Thruster 1 16128 03 Feb 22 @ 18:00:00
Thruster 2 15696
Thruster 3 20016
Thruster 4 20448
Post-Burn
Thruster 1 16528 06 Feb 22 @ 23:30:00
Thruster 2 16064
Thruster 3 20432
Thruster 4 20896
Number of Pulses
Thruster 1 400
Thruster 2 368
Thruster 3 416
Thruster 4 448
Thruster Pairs
Thruster 1 & 2 768
Thruster 3 & 4 864
Timothy E.Perry
CRS IBEX OCO-2
Mission Operations
timothy.perry@ngc.com
Office (703) 406-5976
Cell (301) 606-1430