All,

   The perigee contacts were nominal. The inertial maneuver was successful. The SSR was dumped. During the Flight Computer reset recovery we had sockets fail during an ATS upload. We determined which commands made it onboard and created a Version #2 ats for Orbit 548. The ATS’s  Orbit 548 Version #2 and Orbit 549 were uplinked.  

 

Tasks accomplished:

CAR # 1208 Orbit 548 Version #2 ATS uplink

    IBEX_2021_319_o0548a_V002 76 Cmds

CAR # 1209 Orbit 549  ATS uplink

    IBEX_2021_329_o0549a_V001 88 Cmds

SSR Dump -> Dump New

 

Results from the Inertial Maneuver:

Q1 0.72084900 ActNor.EstInrToBdy[0]

Q2 -0.36486000 ActNor.EstInrToBdy[1]

Q3 -0.15284100 ActNor.EstInrToBdy[2]

Q4 0.56911700 ActNor.EstInrToBdy[3]

     

GPS sec 1321084859 ActNor.EstTime

     

UTC time 11/16/2021 08:00:45 output

MPS Diff 0.802 deg

MPS Cmd Vector X -0.628645000

MPS Cmd Vector Y -0.709905000

MPS Cmd Vector Z -0.317553000

CSS Angle TLM 2.75

CSS Sun-Pointing Angle 5.5

  14 Oct 21 @ 05:00:00

CSS Angle TLM 0.493372

CSS Sun-Pointing Angle 0.986744

  16 Oct 21 @ 08:00:00

Pre-Burn   

Thruster 1 11248 14 Oct 21 @ 05:00:00

Thruster 2 10944

Thruster 3 13728

Thruster 4 14032

Post-Burn  

Thruster 1 11520 16 Oct 21 @ 08:00:00

Thruster 2 11216

Thruster 3 14032

Thruster 4 14336

Number of Pulses  

Thruster 1 272

Thruster 2 272

Thruster 3 304

Thruster 4 304

Thruster Pairs  

Thruster 1 & 2 544

Thruster 3 & 4 608

 

Timothy E.Perry

CRS IBEX OCO-2

Mission Operations

timothy.perry@ngc.com

Office (703) 406-5976

Cell (301) 606-1430

 

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