All,
The perigee Contacts were nominal. The sun maneuver was successful. I was not able to set the static z rate on this contact. The Star percent valid was only at 37%. The Hi instrument sweep table was commanded back to normal sweep.
The Orbit 542 & 543 ATS’s were uploaded. The SSR was dumped and the 18 day timer was reset back to zero.
Tasks Accomplished:
CAR #1152 IBEX Background Tests and Lo Magnetotail Season
Pass # 4 was completed Hi Sweep table set to normal
CAR #1191 Dump Orbit 540 blocks before Flight Computer Reset
CAR #1188 Upload ATS Orbit #542
CAR #1194 Upload ATS Orbit #544
SSR Dump -> Dump New
Reset 18 Day Timer
Results from the Sun Maneuver:
CSS Angle TLM 1.844
CSS Sun-Pointing Angle 3.688
19 Sept 21 @ 01:00:00
CSS Angle TLM 1.024
CSS Sun-Pointing Angle 2.048
23 Sept 21 @ 07:00:00
Pre-Burn
Thruster 1 8608 19 Sept 21 @ 01:00:00
Thruster 2 8416
Thruster 3 9552
Thruster 4 9744 0
Post-Burn
Thruster 1 8960 23 Sept 21 @ 07:00:00
Thruster 2 8720
Thruster 3 10128
Thruster 4 10368
Number of Pulses
Thruster 1 352
Thruster 2 304
Thruster 3 576
Thruster 4 624
Thruster Pairs
Thruster 1 & 2 656
Thruster 3 & 4 1200
Timothy E.Perry
CRS IBEX OCO-2
Mission Operations
timothy.perry@ngc.com
Office (703) 406-5976
Cell (301) 606-1430