All,

    The perigee Contacts were nominal. The sun maneuver was successful. I was not able to set the static z rate on this contact. The Star percent valid was only at 37%. The Hi instrument sweep table was commanded back to normal sweep. The Orbit 542 & 543 ATS’s were uploaded. The SSR was dumped and the 18 day timer was reset back to zero.

 

Tasks Accomplished:

CAR #1152 IBEX Background Tests and Lo Magnetotail Season

    Pass # 4 was completed Hi Sweep table set to normal

CAR #1191 Dump Orbit 540 blocks before Flight Computer Reset

CAR #1188 Upload ATS Orbit #542

CAR #1194 Upload ATS Orbit #544

SSR Dump -> Dump New

Reset 18 Day Timer

 

 

Results from the Sun Maneuver:

CSS Angle TLM 1.844

CSS Sun-Pointing Angle 3.688

  19 Sept 21 @ 01:00:00

CSS Angle TLM 1.024

CSS Sun-Pointing Angle 2.048

  23 Sept 21 @ 07:00:00

Pre-Burn   

Thruster 1 8608 19 Sept 21 @ 01:00:00

Thruster 2 8416

Thruster 3 9552

Thruster 4 9744 0

Post-Burn  

Thruster 1 8960 23 Sept 21 @ 07:00:00

Thruster 2 8720

Thruster 3 10128

Thruster 4 10368

Number of Pulses  

Thruster 1 352

Thruster 2 304

Thruster 3 576

Thruster 4 624

Thruster Pairs 

Thruster 1 & 2 656

Thruster 3 & 4 1200

 

 

 

 

Timothy E.Perry

CRS IBEX OCO-2

Mission Operations

timothy.perry@ngc.com

Office (703) 406-5976

Cell (301) 606-1430

 

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