All,
The spacecraft is nominal. The inertial maneuver was successful. The Orbit #541 ATS was uplinked. The SSR was dumped for orbit 539 and the partial redump was also performed.
Tasks Accomplished:
CAR #1185 – Redump initial orbit 539 blocks
CAR #1187 – Orbit 541 ATS uplink – IBEX_2021_257_o0541a_v001 – 96 Cmds
Reset the 18 DAY timer
SSR Dump -> Dump New
Results from the Inertial Maneuver:
Q1 0.28713500 ActNor.EstInrToBdy[0]
Q2 -0.59108400 ActNor.EstInrToBdy[1]
Q3 -0.52607500 ActNor.EstInrToBdy[2]
Q4 0.53983200 ActNor.EstInrToBdy[3]
GPS sec 1314906224 ActNor.EstTime
UTC time
09/05/2021 19:43:30 output
MPS Cmd Vector X -0.942244000
MPS Cmd Vector Y 0.310760000
MPS Cmd Vector Z 0.124918000
MPS Diff
0.668 deg
CSS Angle TLM
1.74125
CSS Sun-Pointing Angle
3.4825
01 Sept 21 @ 03:00:00
CSS Angle TLM
1.537
CSS Sun-Pointing Angle
3.074
05 Sept 21 @ 19:\30:00
Pre-Burn
Thruster 1
7536 01 Sept 21 @ 03:00:00
Thruster 2
7376
Thruster 3
8384
Thruster 4
8544
Post-Burn
Thruster 1
7808 05 Sept 21 @ 19:\30:00
Thruster 2
7648
Thruster 3
8672
Thruster 4
8832
Number of Pulses
Thruster 1
272
Thruster 2
272
Thruster 3
288
Thruster 4
288
Thruster Pairs
Thruster 1 & 2
544
Thruster 3 & 4
576
Timothy E.Perry
CRS IBEX OCO-2
Mission Operations
timothy.perry@ngc.com
Office (703) 406-5976
Cell (301) 606-1430