All,
The spacecraft was nominal. The inertial maneuver was successful. Orbit 640 ATS was uplinked.
Tasks accomplished:
CAR #1186 Orbit#540 ATS uplink
IBEX_2021_248_o0540a_v001 93cmds
Results from the Inertial maneuver:
Q1 -0.05612130 ActNor.EstInrToBdy[0]
Q2 -0.64456200 ActNor.EstInrToBdy[1]
Q3 -0.22859100 ActNor.EstInrToBdy[2]
Q4 0.72741800 ActNor.EstInrToBdy[3]
GPS sec 1314500505 ActNor.EstTime
UTC time
09/01/2021 03:01:31 output
MPS Diff
0.601 deg
MPS Cmd Vector X -0.913727000
MPS Cmd Vector Y 0.376667000
MPS Cmd Vector Z 0.152399000
CSS Angle TLM 0.521
CSS Sun-Pointing Angle 1.042
27 Aug 21 @ 16:00:00
CSS Angle TLM 1.74125
CSS Sun-Pointing Angle 3.4825
01 Sept 21 @ 03:00:00
Pre-Burn
Thruster 1 7264 27 Aug 21 @ 16:00:00
Thruster 2 7104
Thruster 3 8080
Thruster 4 8240
Post-Burn
Thruster 1 7536 01 Sept 21 @ 03:00:00
Thruster 2 7376
Thruster 3 8384
Thruster 4 8544
Number of Pulses
Thruster 1 272
Thruster 2 272
Thruster 3 304
Thruster 4 304
Thruster Pairs
Thruster 1 & 2 544
Thruster 3 & 4 608
Timothy E.Perry
CRS IBEX OCO-2
Mission Operations
timothy.perry@ngc.com
Office (703) 406-5976
Cell (301) 606-1430