All,
The perigee contacts were nominal for CMD & TLM. The inertial maneuver was successful.
We were able to dump the SSR for this orbit and redump the data from orbit536. The ATS for Orbit #539 has been uplinked. The clock has been set and FDC totals were reset. The
18 day master timer was reset back to zero.
Tasks Accomplished:
CAR #1183 – Redump Orbit 538 SSR
CAR # 1184 – Orbit #539 ATS
IBEX_2021_239_o0539a_v001 93 cmds
SSR Dump -> Dump New
Reset Master Timer
Set Spacecraft Clock
Reset FDC totals
Results from the Inertial Maneuver:
Q1 -0.21962800 ActNor.EstInrToBdy[0]
Q2 -0.57569400 ActNor.EstInrToBdy[1]
Q3 -0.18919800 ActNor.EstInrToBdy[2]
Q4 0.76455500 ActNor.EstInrToBdy[3]
GPS sec 1313345842 ActNor.EstTime
UTC time
08/18/2021 18:17:08 output
MPS Cmd Vector X -0.799940000
MPS Cmd Vector Y 0.554091000
MPS Cmd Vector Z 0.230389000
MPS Diff
0.611 deg
CSS Angle TLM
0.301965
CSS Sun-Pointing Angle
0.60393
14 Aug 21 @ 03:00:00
CSS Angle TLM
0.290066
CSS Sun-Pointing Angle
0.580132
18 Aug 21 @ 18:00:00
Pre-Burn
Thruster 1
6480 14 Aug 21 @ 03:00:00
Thruster 2
6352
Thruster 3
7200
Thruster 4
7328
Post-Burn
Thruster 1
6752 18 Aug 21 @ 18:00:00
Thruster 2
6592
Thruster 3
7504
Thruster 4
7664
Number of Pulses
Thruster 1
272
Thruster 2
240
Thruster 3
304
Thruster 4
336
Thruster Pairs
Thruster 1 & 2
512
Thruster 3 & 4
640
Timothy E.Perry
CRS IBEX OCO-2
Mission Operations
timothy.perry@ngc.com
Office (703) 406-5976
Cell (301) 606-1430