All,
The perigee contacts were nominal for CMD & TLM. The inertial maneuver was successful. The Orbit 534 ATS was uplinked. The SSR was dumped and the 18 day master timer was reset.
Tasks Accomplished:
CAR #1177 Orbit #534 ATS uplink
IBEX_2021_194_o0534a_v001 93 CMDS
Reset master timer
SSR Dump -> Dump New
Set Spacecraft Time
Results from the Inertial Maneuver:
Q1 -0.55112000 ActNor.EstInrToBdy[0]
Q2 -0.01182710 ActNor.EstInrToBdy[1]
Q3 0.13360400 ActNor.EstInrToBdy[2]
Q4 0.82357600 ActNor.EstInrToBdy[3]
GPS sec 1309381933 ActNor.EstTime
UTC time
07/03/2021 21:11:59 output
MPS Diff
0.563 deg
MPS Cmd Vector X -0.170334000
MPS Cmd Vector Y 0.907633000
MPS Cmd Vector Z 0.383651000
CSS Angle TLM 1.68992
CSS Sun-Pointing Angle 3.37984
29 June 21 @ 12:00:00
CSS Angle TLM 1.1955
CSS Sun-Pointing Angle 2.391
03 July 21 @ 21:00:00
Pre-Burn
Thruster 1 3824 29 June 21 @ 12:00:00
Thruster 2 3760
Thruster 3 4256
Thruster 4 4320
Post-Burn
Thruster 1 4096 03 July 21 @ 21:00:00
Thruster 2 4000
Thruster 3 4528
Thruster 4 4624
Number of Pulses
Thruster 1 272
Thruster 2 240
Thruster 3 272
Thruster 4 304
Thruster Pairs
Thruster 1 & 2 512
Thruster 3 & 4 576
Timothy E.Perry
CRS IBEX OCO-2
Mission Operations
timothy.perry@ngc.com
Office (703) 406-5976
Cell (301) 606-1430