All,
The perigee contacts were nominal for CMD & TLM. The inertial maneuver and master reset commands executed successfully. SSR was dumped for the previous orbit and a redump
for Orbit 526.
The following objectives were accomplished:
1.
CAR #1170 SSR_Re-Dump Orbit# o0526
2.
CAR #1171 Upload Orbit# 529 ATS
a.
Bus: IBEX_2021_148_o0529a_BUS_v001 (376-428)
b.
Inst; IBEX_2021_148_o0529a_INST_v001 (429-474)
3.
SSR_Dump (NEW)
4.
Dump_Backorbit
Results from the Inertial Maneuver:
Q1 0.01660470 ActNor.EstInrToBdy[0]
Q2 0.57764600 ActNor.EstInrToBdy[1]
Q3 0.66728500 ActNor.EstInrToBdy[2]
Q4 0.46987200 ActNor.EstInrToBdy[3]
GPS sec 1305471770 ActNor.EstTime
UTC time
05/19/2021 15:02:36 output
MPS Cmd Vector X 0.560428000
MPS Cmd Vector Y 0.763405000
MPS Cmd Vector Z 0.321142000
MPS Diff
0.826 deg
CSS Angle TLM
0.65132
CSS Sun-Pointing Angle
1.30264
14 Apr 21 @ 12:00:00
CSS Angle TLM
0.586842
CSS Sun-Pointing Angle
1.173684
19 Apr 21 @ 15:00:00
Pre-Burn
Thruster 1
1120 14 Apr 21 @ 12:00:00
Thruster 2
1088
Thruster 3
1200
Thruster 4
1232
Post-Burn
Thruster 1
1408 19 Apr 21 @ 15:00:00
Thruster 2
1376
Thruster 3
1520
Thruster 4
1552
Number of Pulses
Thruster 1
288
Thruster 2
288
Thruster 3
320
Thruster 4
320
Thruster Pairs
Thruster 1 & 2
576
Thruster 3 & 4
640
Timothy E.Perry
CRS IBEX OCO-2
Mission Operations
timothy.perry@ngc.com
Office (703) 406-5976
Cell (301) 606-1430