All,
The Apogee contact was nominal for CMD & TLM. The Inertial maneuver was successful. The extra Comm pass ATS was uplinked, FC Back orbit data was dumped and the FDC totals
were reset.
Tasks Accomplished:
CAR #1169 Orbit 527 Comm pass ATS
Reset FDC Totals
Dumped FC Back Orbit data
Results from the Inertial Maneuver:
Q1 -0.10149300 ActNor.EstInrToBdy[0]
Q2 0.57799700 ActNor.EstInrToBdy[1]
Q3 0.50432500 ActNor.EstInrToBdy[2]
Q4 0.63346200 ActNor.EstInrToBdy[3]
GPS sec 1305029080 ActNor.EstTime
UTC time
05/14/2021 12:04:26 output
MPS Cmd Vector X 0.624788000
MPS Cmd Vector Y 0.720309000
MPS Cmd Vector Z 0.301322000
MPS Diff
0.812 deg
CSS Angle TLM
0.330431
CSS Sun-Pointing Angle
0.660862
10Apr 21 @ 10:00:00
CSS Angle TLM
0.65132
CSS Sun-Pointing Angle
1.30264
14 Apr 21 @ 12:00:00
Pre-Burn
Thruster 1
816 10Apr 21 @ 10:00:00
Thruster 2
816
Thruster 3
928
Thruster 4
928
Post-Burn
Thruster 1
1120 14 Apr 21 @ 12:00:00
Thruster 2
1088
Thruster 3
1200
Thruster 4
1232
Number of Pulses
Thruster 1
304
Thruster 2
272
Thruster 3
272
Thruster 4
304
Thruster Pairs
Thruster 1 & 2
576
Thruster 3 & 4
576
Timothy E.Perry
CRS IBEX OCO-2
Mission Operations
timothy.perry@ngc.com
Office (703) 406-5976
Cell (301) 606-1430