All,
The perigee contacts were nominal for CMD& TLM. The inertial maneuver was successful. The ATS’s for Orbit #528 have been uplinked. The SSR and the Flight Computer Back Orbit
data has been dumped. The SSR was dumped thru APL and waiting for the files to come across for archiving. The 18 day timer command executed nominally and the timer was set back to 10.
Tasks Accomplished:
CAR #4528 – Orbit#528 ATS upload
IBEX_2021_139_o0528a_BUS_V001
IBEX_2021_139_o0528a_INST_V001
Reset FDC Totals
Dumped Flight Computer Back Orbit Data
Results from the Inertial Maneuver:
Q1 -0.56903500 ActNor.EstInrToBdy[0]
Q2 -0.17848200 ActNor.EstInrToBdy[1]
Q3 -0.71675300 ActNor.EstInrToBdy[2]
Q4 0.36139900 ActNor.EstInrToBdy[3]
GPS sec 1304676106 ActNor.EstTime
UTC time
05/10/2021 10:01:32 output
MPS Cmd Vector X 0.683656000
MPS Cmd Vector Y 0.673118000
MPS Cmd Vector Z 0.282007000
MPS Diff
0.538 deg
CSS Angle TLM 0.874469
CSS Sun-Pointing Angle 1.748938
06Apr 21 @ 12:00:00
CSS Angle TLM 0.330431
CSS Sun-Pointing Angle 0.660862
10Apr 21 @ 10:00:00
Pre-Burn
Thruster 1 544 06Apr 21 @ 12:00:00
Thruster 2 544
Thruster 3 608
Thruster 4 608
Post-Burn
Thruster 1 816 10Apr 21 @ 10:00:00
Thruster 2 816
Thruster 3 928
Thruster 4 928
Number of Pulses
Thruster 1 272
Thruster 2 272
Thruster 3 320
Thruster 4 320
Thruster Pairs
Thruster 1 & 2 544
Thruster 3 & 4 640
Timothy E.Perry
CRS IBEX OCO-2
Mission Operations
timothy.perry@ngc.com
Office (703) 406-5976
Cell (301) 606-1430