All,

    The perigee contacts were nominal for CMD & TLM. The Inertial maneuver was successful. The Orbit 523 Hi Gain Cal ATS and the Orbit 524 Bus ATS was uplinked. The spacecraft clock was set. I was also able to redump the missing data from Orbit #521. The 18 day timer reset command executed nominally. The number of timed commands onboard at LOS was 203.

 

Tasks Accomplished:

Reset FDC Totals

Set Spacecraft Clock

SSR Dump -> Dump New

CAR #1158 – Orbit #521 SSR Redump

CAR #1159 – Orbit #524 ATS upload

    IBEX_2021_103_o0524a_BUS_V001 53 Cmds

CAR #1160 – Orbit #523 Hi Gain Cal ATS

     IBEX_2021_093_o0523a_HGC_v001

 

 

Results from the Inertial Maneuver:

Q1 0.60847600 ActNor.EstInrToBdy[0]

Q2 0.30404200 ActNor.EstInrToBdy[1]

Q3 0.70253300 ActNor.EstInrToBdy[2]

Q4 0.20919500 ActNor.EstInrToBdy[3]

     

GPS sec 1301440471 ActNor.EstTime

     

UTC time 04/02/2021 23:14:17 output

MPS Diff 0.507 deg

MPS Cmd Vector X 0.981968000

MPS Cmd Vector Y 0.176826000

MPS Cmd Vector Z 0.066866000

CSS Angle TLM 0.473953

CSS Sun-Pointing Angle 0.947906

  29 Mar 21 @ 13:00:00

CSS Angle TLM 0.0279765

CSS Sun-Pointing Angle 0.055953

  02 Apr 21 @ 23:00:00

Pre-Burn   

Thruster 1 4394 29 Mar 21 @ 13:00:00

Thruster 2 4256

Thruster 3 5952

Thruster 4 6080

Post-Burn  

Thruster 1 4704 02 Apr 21 @ 23:00:00

Thruster 2 4544

Thruster 3 6288

Thruster 4 6448

Number of Pulses  

Thruster 1 310

Thruster 2 288

Thruster 3 336

Thruster 4 368

Thruster Pairs 

Thruster 1 & 2 598

Thruster 3 & 4 704

 

 

 

Timothy E.Perry

CRS IBEX OCO-2

Mission Operations

timothy.perry@ngc.com

Office (703) 406-5976

Cell (301) 606-1430

 

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