All,
The perigee contacts were nominal for CMD & TLM. The Inertial maneuver was successful. The Orbit 523 Hi Gain Cal ATS and the Orbit 524 Bus ATS was uplinked. The spacecraft
clock was set. I was also able to redump the missing data from Orbit #521. The 18 day timer reset command executed nominally. The number of timed commands onboard at LOS was 203.
Tasks Accomplished:
Reset FDC Totals
Set Spacecraft Clock
SSR Dump -> Dump New
CAR #1158 – Orbit #521 SSR Redump
CAR #1159 – Orbit #524 ATS upload
IBEX_2021_103_o0524a_BUS_V001 53 Cmds
CAR #1160 – Orbit #523 Hi Gain Cal ATS
IBEX_2021_093_o0523a_HGC_v001
Results from the Inertial Maneuver:
Q1 0.60847600 ActNor.EstInrToBdy[0]
Q2 0.30404200 ActNor.EstInrToBdy[1]
Q3 0.70253300 ActNor.EstInrToBdy[2]
Q4 0.20919500 ActNor.EstInrToBdy[3]
GPS sec 1301440471 ActNor.EstTime
UTC time
04/02/2021 23:14:17 output
MPS Diff
0.507 deg
MPS Cmd Vector X 0.981968000
MPS Cmd Vector Y 0.176826000
MPS Cmd Vector Z 0.066866000
CSS Angle TLM 0.473953
CSS Sun-Pointing Angle 0.947906
29 Mar 21 @ 13:00:00
CSS Angle TLM 0.0279765
CSS Sun-Pointing Angle 0.055953
02 Apr 21 @ 23:00:00
Pre-Burn
Thruster 1 4394 29 Mar 21 @ 13:00:00
Thruster 2 4256
Thruster 3 5952
Thruster 4 6080
Post-Burn
Thruster 1 4704 02 Apr 21 @ 23:00:00
Thruster 2 4544
Thruster 3 6288
Thruster 4 6448
Number of Pulses
Thruster 1 310
Thruster 2 288
Thruster 3 336
Thruster 4 368
Thruster Pairs
Thruster 1 & 2 598
Thruster 3 & 4 704
Timothy E.Perry
CRS IBEX OCO-2
Mission Operations
timothy.perry@ngc.com
Office (703) 406-5976
Cell (301) 606-1430