All,

   The perigee contacts were nominal for CMD and TLM. The Inertial maneuver was successful. The SSR dump was successful during the first contact. I also dumped the SSR during the second contact. The Instrument ATS for Orbit 498 was uplinked. 18 Day timer command executed and counter was reset to 10. Deleted stored commands for APL and the SSC contact on 08/09/2020@19:00gmt.

 

Tasks Accomplished:

CAR #1106 ATS upload

    IBEX_2020_232_o0498a_INST_V001 46 cmds

SSR Dump -> Dump New (2ea)

Set Spacecraft Clock

Deleted Timed commands for APL and original SSC contact. on 08/09/2020@19:00gmt

 

Results for the Inertial maneuver:

Q1 -0.47604600 ActNor.EstInrToBdy[0]

Q2 -0.36396800 ActNor.EstInrToBdy[1]

Q3 0.13841600 ActNor.EstInrToBdy[2]

Q4 0.78851100 ActNor.EstInrToBdy[3]

GPS sec 1281031399 ActNor.EstTime

UTC time 08/09/2020 18:03:05 output

MPS Diff 0.511 deg

MPS Cmd Vector X -0.705841000

MPS Cmd Vector Y 0.653433000

MPS Cmd Vector Z 0.273523000

CSS Angle TLM 0.77718

CSS Sun-Pointing Angle 1.55436

  5 Aug 20 @ 11:00

CSS Angle TLM 0.239031

CSS Sun-Pointing Angle 0.478062

  9 Aug 20 @ 17:00

Pre-Burn   

Thruster 1 1712 5 Aug 20 @ 11:00

Thruster 2 1680

Thruster 3 2000

Thruster 4 2032

Post-Burn   `

Thruster 1 2000 9 Aug 20 @ 17:00

Thruster 2 1936

Thruster 3 2304

Thruster 4 2368

Number of Pulses  

Thruster 1 288

Thruster 2 256

Thruster 3 304

Thruster 4 336

Thruster Pairs 

Thruster 1 & 2 544

Thruster 3 & 4 640

 

 

 

 

Timothy E. Perry

Mission Operations

CRS, IBEX, OCO-2

timothy.perry@ngc.com

Office (703) 406-5976

Cell (301) 606-1430