All,
The perigee passes were nominal for CMD and TLM. The Inertial maneuver was successful. The SSR and Flight Computer Back Orbit Buffer was dumped. The 18 Day Master Timer reset
command executed and the count back to 10.
Results from the Inertial Maneuver:
Q1 0.01592180 ActNor.EstInrToBdy[0]
Q2 -0.55725000 ActNor.EstInrToBdy[1]
Q3 -0.78861700 ActNor.EstInrToBdy[2]
Q4 0.25942600 ActNor.EstInrToBdy[3]
GPS sec 1278602641 ActNor.EstTime
MPS Cmd Vector X -0.316162000
MPS Cmd Vector Y 0.873961000
MPS Cmd Vector Z 0.369098000
MPS Diff
0.579 deg
CSS Angle TLM
1.50024
CSS Sun-Pointing Angle
3.00048
9 July 20 @ 12:00
CSS Angle TLM
0.488189
CSS Sun-Pointing Angle
0.976378
12 July 20 @ 14:30
Pre-Burn
Thruster 1
112 8 July 20 @ 12:00
Thruster 2
112
Thruster 3
144
Thruster 4
144
Post-Burn
Thruster 1
368 12 July 20 @ 14:30
Thruster 2
368
Thruster 3
480
Thruster 4
480
Number of Pulses
Thruster 1
256
Thruster 2
256
Thruster 3
336
Thruster 4
336
Thruster Pairs
Thruster 1 & 2
512
Thruster 3 & 4
672
Timothy E.Perry
CRS IBEX OCO-2
Mission Operations
timothy.perry@ngc.com
Office (703) 406-5976
Cell (301) 606-1430