All,
The perigee contacts were nominal for CMD and TLM. The inertial maneuver was successful. The Hi background test was completed and orbit 494 Bus ATS was uploaded.
Tasks Accomplished:
SSR Dump -> Dump New
CAR #1099 Hi Background Test completed
CAR #2003 ATS upload – IBEX_2020_194_o0494a_BUS_V001 48 cmds
Results from the Inertial maneuver:
Q1 -0.51404600 ActNor.EstInrToBdy[0]
Q2 -0.19255300 ActNor.EstInrToBdy[1]
Q3 -0.28182200 ActNor.EstInrToBdy[2]
Q4 0.78692900 ActNor.EstInrToBdy[3]
GPS sec 1277095426 ActNor.EstTime
UTC time 06/25/2020 04:43:32 output
MPS Diff 0.602 deg
MPS Cmd Vector X -0.019289000
MPS Cmd Vector Y 0.920861000
MPS Cmd Vector Z 0.389413000
CSS Angle TLM 1.62148
CSS Sun-Pointing Angle 3.24296
20 June 20 @ 12:00
CSS Angle TLM 2.49
CSS Sun-Pointing Angle 4.98
24 June 20 @ 15:00
Pre-Burn
Thruster 1 11328 20 June 20 @ 12:00
Thruster 2 11024
Thruster 3 14080
Thruster 4 14384
Post-Burn
Thruster 1 11600 24 June 20 @ 15:00
Thruster 2 11296
Thruster 3 14386
Thruster 4 14672
Number of Pulses
Thruster 1 272
Thruster 2 272
Thruster 3 306
Thruster 4 288
Thruster Pairs
Thruster 1 & 2 544
Thruster 3 & 4 594
Timothy E.Perry
CRS IBEX OCO-2
Mission Operations
timothy.perry@ngc.com
Office (703) 406-5976
Cell (301) 606-1430