All,

   The perigee contacts were nominal for CMD and TLM. The Inertial maneuver was successful. The Instrument ATS for Orbit 491 was uplinked. At LOS there were 226 stored commands onboard. The Master Reset timer reset to zero thru stored command.  

 

The following was accomplished:

CAR 2000 ATS upload – Ibex_2020_167_o0491a_INST_V001 46 CMDS

SSR Dump –Dump New

Set Spacecraft Clock

Reset FDC Counters

 

 

Q1 -0.27220500 ActNor.EstInrToBdy[0]

Q2 0.48259500 ActNor.EstInrToBdy[1]

Q3 0.56508900 ActNor.EstInrToBdy[2]

Q4 0.61129500 ActNor.EstInrToBdy[3]

MPS Cmd Vector X 0.279738000

MPS Cmd Vector Y 0.884416000

MPS Cmd Vector Z 0.373571000

GPS sec 1275516331 ActNor.EstTime

UTC time 06/06/2020 22:05:17 output

MPS Diff 0.810 deg

CSS Angle TLM 1.45804

CSS Sun-Pointing Angle 2.91608

  02 May 20 @07:00

CSS Angle TLM 0.958588

CSS Sun-Pointing Angle 1.917176

  06 May 20 @22:00

Pre-Burn  

Thruster 1 10240 02 May 20 @07:00

Thruster 2 9968

Thruster 3 12912

Thruster 4 13184

Post-Burn  

Thruster 1 10544 06 May 20 @22:00

Thruster 2 10240

Thruster 3 13216

Thruster 4 13520

Number of Pulses  

Thruster 1 304

Thruster 2 272

Thruster 3 304

Thruster 4 336

Thruster Pairs 

Thruster 1 & 2 576

Thruster 3 & 4 640

 

 

 

 

Timothy E. Perry

Mission Operations

CRS, IBEX, OCO-2

timothy.perry@ngc.com

Office (703) 406-5976

Cell (301) 606-1430