All,

   The perigee contact was nominal for CMD and TLM. The Inertial maneuver was successful. The Bus ATS for Orbit# 492 was uplinked. Stored Command count is at 216.

 

The following was accomplished:

CAR #2001 ATS upload – IBEX_2020_176_o0492a_BUS_V001 48 CMDS

 

 

Results for the Inertial maneuver:

Q1 -0.51258000 ActNor.EstInrToBdy[0]

Q2 -0.22654900 ActNor.EstInrToBdy[1]

Q3 -0.60121800 ActNor.EstInrToBdy[2]

Q4 0.56962600 ActNor.EstInrToBdy[3]

MPS Cmd Vector X 0.351388000

MPS Cmd Vector Y 0.862943000

MPS Cmd Vector Z 0.363121000

GPS sec 1275130986 ActNor.EstTime

UTC time 06/02/2020 11:02:52 output

MPS Diff 0.738 deg

CSS Angle TLM 0.569926

CSS Sun-Pointing Angle 1.139852

  29 May 20 @01:30

CSS Angle TLM 1.45804

CSS Sun-Pointing Angle 2.91608

  02 May 20 @07:00

Pre-Burn   

Thruster 1 9984 29 May 20 @01:30

Thruster 2 9712

Thruster 3 12640

Thruster 4 12912

Post-Burn  

Thruster 1 10240 02 May 20 @07:00

Thruster 2 9968

Thruster 3 12912

Thruster 4 13184

Number of Pulses  

Thruster 1 256

Thruster 2 256

Thruster 3 272

Thruster 4 272

Thruster Pairs 

Thruster 1 & 2 512

Thruster 3 & 4 544

 

 

 

 

Timothy E. Perry

Mission Operations

CRS, IBEX, OCO-2

timothy.perry@ngc.com

Office (703) 406-5976

Cell (301) 606-1430