All,

    The perigee contacts were nominal for CMD and TLM. The Inertial maneuver was successful.

The Instrument ATS for orbit #488 was uploaded during the USAK01 contact on 11 May @00:30gmt.

Total commands on board at LOS were 228. The Master reset timer reset command executed @01:15:00 and was verified @01:25:00.

 

Note: the ATS’s for orbit#490 will be sent out on 11 May.

 

The following was accomplished:

Reset FDC Totals

Set Spacecraft Time

SSR Dump -> Dump New

CAR# 1096 ATS upload -> IBEX_2020_140_o0488a_INST_V001 46 Cmds

 

Results from the Inertial Maneuver:

 

Q1 0.09546380 ActNor.EstInrToBdy[0]

Q2 0.58523000 ActNor.EstInrToBdy[1]

Q3 0.65442300 ActNor.EstInrToBdy[2]

Q4 0.46910200 ActNor.EstInrToBdy[3]

GPS sec 1273192202 ActNor.EstTime

UTC time 05/11/2020 00:29:48 output

MPS Cmd Vector X 0.669273000

MPS Cmd Vector Y 0.685255000

MPS Cmd Vector Z 0.287227000

MPS Diff 0.791 deg

CSS Angle TLM 0.359365

CSS Sun-Pointing Angle 0.71873

  06 May 20 @ 03:00

CSS Angle TLM 0.359909

CSS Sun-Pointing Angle 0.719818

  11 May 20 @ 00:30

Pre-Burn   

Thruster 1 8672 06 May 20 @ 03:00

Thruster 2 8400

Thruster 3 11216

Thruster 4 11488

Post-Burn  

Thruster 1 8928 11 May 20 @ 00:30

Thruster 2 8656

Thruster 3 11488

Thruster 4 11760

Number of Pulses  

Thruster 1 256

Thruster 2 256

Thruster 3 272

Thruster 4 272

Thruster Pairs  

Thruster 1 & 2 512

Thruster 3 & 4 544

 

 

 

 

Timothy E. Perry

Mission Operations

CRS, IBEX, OCO-2 & TESS

timothy.perry@ngc.com

Office (703) 406-5976

Cell (301) 606-1430