All,
The perigee contacts were nominal for CMD and TLM. The inertial maneuver was successful. The Master Timer was reset to 0 via timed command on 23April2020 @05:45:00. The bus
ATS’s for orbit’s 487 and 488 has been uplinked. The current command count is @226.
The following was accomplished:
SSR Dump -> Dump new and reset pointers.
Reset FDC Totals
Verified Master Timer Reset 23April2020 @05:45:00
CAR # 1095 ATS upload – IBEX_2020_133_o0487_BUS_V001 41 Cmds
CAR # 1096 ATS upload – IBEX_2020_140_o0488_BUS_V001 48 Cmds
Results from the Inertial Maneuver:
Q1 -0.63153800 ActNor.EstInrToBdy[0]
Q2 0.00257630 ActNor.EstInrToBdy[1]
Q3 -0.68173000 ActNor.EstInrToBdy[2]
Q4 0.36932000 ActNor.EstInrToBdy[3]
GPS sec 1271653218 ActNor.EstTime
UTC time 04/23/2020 05:00:04 output
MPS Cmd Vector X 0.859739000
MPS Cmd Vector Y 0.472118000
MPS Cmd Vector Z 0.194816000
MPS Diff
0.703 deg
CSS Angle TLM
0.889115
CSS Sun-Pointing Angle
1.77823
19 Apr 20 @ 13:00
CSS Angle TLM
0.387149
CSS Sun-Pointing Angle
0.774298
23 Apr 20 @ 05:00
Pre-Burn
Thruster 1
7664 19 Apr 20 @ 13:00
Thruster 2
7440
Thruster 3
9952
Thruster 4
10176
Post-Burn
Thruster 1
7968 23 Apr 20 @ 05:00
Thruster 2
7696
Thruster 3
10256
Thruster 4
10528
Number of Pulses
Thruster 1
304
Thruster 2
256
Thruster 3
304
Thruster 4
352
Thruster Pairs
Thruster 1 & 2
560
Thruster 3 & 4
656
Timothy E.Perry
CRS IBEX OCO-2
Mission Operations
timothy.perry@ngc.com
Office (703) 406-5976
Cell (301) 606-1430