All,

   The Perigee passes were nominal for CMD and TLM. The Inertial maneuver was successful. The 18 day master timer command was sent as a timed command for future planning reference. The command was successful.

 

The following was completed:

Reset Master Timer

Reset FDC Totals

CAR # 1091 ATS upload IBEX_2020_105_o0484a_v001 96 CMDs

SSR Dump -> Dump New

Set Spacecraft time

EMR_StrobeMReset $Time=2020/04:05:15:08:00

 

 

 

Results from the Inertial Maneuver:

Q1 0.05583000 ActNor.EstInrToBdy[0]

Q2 0.67101200 ActNor.EstInrToBdy[1]

Q3 0.21208700 ActNor.EstInrToBdy[2]

Q4 0.70826900 ActNor.EstInrToBdy[3]

MPS Cmd Vector X 0.972761000

MPS Cmd Vector Y 0.216101000

MPS Cmd Vector Z 0.083887000

GPS sec 1270096268 ActNor.EstTime

UTC time 04/05/2020 04:30:54 output

CSS Angle TLM 0.148033

CSS Sun-Pointing Angle 0.296066

  31 Mar 20 @ 13:00

CSS Angle TLM 0.260196

CSS Sun-Pointing Angle 0.520392

  5 Apr 20 @ 4:30

Pre-Burn  

Thruster 1 6608 31 Mar 20 @ 13:00

Thruster 2 6416

Thruster 3 8784

Thruster 4 8976

Post-Burn  

Thruster 1 6848 5 Apr 20 @ 4:30

Thruster 2 6656

Thruster 3 9056

Thruster 4 9248

Number of Pulses  

Thruster 1 240

Thruster 2 240

Thruster 3 272

Thruster 4 272

Thruster Pairs 

Thruster 1 & 2 480

Thruster 3 & 4 544

 

 

 

 

Timothy E. Perry

Mission Operations

CRS, IBEX, OCO-2 & TESS

timothy.perry@ngc.com

Office (703) 406-5976

Cell (301) 606-1430