All,

    The Perigee passes were nominal for CMD and TLM. The Inertial maneuver was successful.

The following was accomplished:

Reset the Master Timer

SSR Dump -> Dump New

CAR #1070 ATS upload – IBEX_2019_314_o0467a_v001 81 Cmds

 

Results from the Inertial maneuver:

Q1 0.75908400

Q2 -0.19473400

Q3 -0.41845700

Q4 0.45909100

   

GPS sec 1256598137

MPS Diff 0.722 deg

MPS Cmd Vector X -0.811712000

MPS Cmd Vector Y -0.532222000

MPS Cmd Vector Z -0.240550000

CSS Angle TLM 0.296075

CSS Sun-Pointing Angle 0.59215

  27 Oct 19 @ 23:00

CSS Angle TLM 1.00112

CSS Sun-Pointing Angle 2.00224

  31 Oct 19 @ 22:15

Pre-Burn   

Thruster 1 19664 27 Oct 19 @ 23:00

Thruster 2 19072

Thruster 3 25328

Thruster 4 25920

Post-Burn  

Thruster 1 19904 31 Oct 19 @ 22:15

Thruster 2 19312

Thruster 3 25632

Thruster 4 26224

Number of Pulses  

Thruster 1 240

Thruster 2 240

Thruster 3 304

Thruster 4 304

Thruster Pairs 

Thruster 1 & 2 480

Thruster 3 & 4 608

 

 

 

 

Timothy E. Perry

Mission Operations

CRS, IBEX, OCO-2 & TESS

timothy.perry@ngc.com

Office (703) 406-5976

Cell (301) 606-1430