All,
The perigee contacts were nominal for CMD & TLM. The Inertial maneuver was successful.
The following was accomplished:
SSR Dump -> Dump New
Reset Master Timer
Set Spacecraft Clock
Reset FDC Totals
Results from the Inertial maneuver:
Q1 0.43030900 ActNor.EstInrToBdy[0]
Q2 -0.47554900 ActNor.EstInrToBdy[1]
Q3 -0.70310300 ActNor.EstInrToBdy[2]
Q4 0.30713700 ActNor.EstInrToBdy[3]
GPS sec 1251201617 ActNor.EstTime
UTC time 08/30/2019 12:00:03 output
MPS Cmd Vector X -0.898903000
MPS Cmd Vector Y 0.405493000
MPS Cmd Vector Z 0.165977000
MPS Diff
0.664 deg
CSS Angle TLM
0.360452
CSS Sun-Pointing Angle
0.720904
25 Aug 19 @ 10:30
CSS Angle TLM
0.336882
CSS Sun-Pointing Angle
0.673764
30 Aug 19 @ 12:00
Pre-Burn
Thruster 1
17056 25 Aug 19 @ 10:30
Thruster 2
16608
Thruster 3
20128
Thruster 4
20576
Post-Burn
Thruster 1
17312 30 Aug 19 @ 12:00
Thruster 2
16864
Thruster 3
20416
Thruster 4
20864
Number of Pulses
Thruster 1
256
Thruster 2
256
Thruster 3
288
Thruster 4
288
Thruster Pairs
Thruster 1 & 2
512
Thruster 3 & 4
576
Timothy E.Perry
CRS IBEX OCO-2
Mission Operations
tim.perry@ngc.com
Office (703) 406-5976
Cell (301) 606-1430