All,
The perigee supports were nominal for CMD and TLM. The inertial maneuver was successful. Battery balancing was nominal.
The following was completed:
CAR #1039 Orbit #450 ATS, Uplinked 93 commands
Reset Master Timer
Dumped the SSR and set the pointers to 70000
VC2 Count = 24615 with 11 sequence errors
Q1 -0.48966000 ActNor.EstInrToBdy[0]
Q2 -0.27621000 ActNor.EstInrToBdy[1]
Q3 -0.66384700 ActNor.EstInrToBdy[2]
Q4 0.49320200 ActNor.EstInrToBdy[3]
GPS sec 1243362568.000 ActNor.EstTime
MPS Diff 0.498 deg
MPS Cmd Vector X 0.377420000
MPS Cmd Vector Y 0.853224000
MPS Cmd Vector Z 0.359948000
CSS Angle TLM 0.26467
CSS Sun-Pointing Angle 0.52934
27 May 19 @ 13:00
CSS Angle TLM 0.323851
CSS Sun-Pointing Angle 0.647702
31 May 19 @ 18:30
Pre-Burn
Thruster 1 11824 27 May 19 @ 13:00
Thruster 2 11536
Thruster 3 14208
Thruster 4 14496
Post-Burn
Thruster 1 12128 31 May 19 @ 18:30
Thruster 2 11808
Thruster 3 14496
Thruster 4 14816
Number of Pulses
Thruster 1 304
Thruster 2 272
Thruster 3 288
Thruster 4 320
Thruster Pairs
Thruster 1 & 2 576
Thruster 3 & 4 608
Eric Chubin
Mission Operations Engineer - OCO2, IBEX
Northrop Grumman Innovation Systems
OCO2 MOC#: (703) 429 - 7015
Mobile#: (240) 328 - 2098
Eric.Chubin@ngc.com