All,
The perigee contacts were nominal for CMD and TLM. The Inertial maneuver was successful and battery balancing was nominal.
The following was completed:
Reset Master Timer
CAR #1017 ATS Upload – IBEX_2019_023_o0435a_v001.scr
SSR Dump
CAR #1016 – Re-dump orbit 432 problem blocks
Results from the Inertial Maneuver:
Q1 0.53833000 ActNor.EstInrToBdy[0]
Q2 -0.62564200 ActNor.EstInrToBdy[1]
Q3 0.54679700 ActNor.EstInrToBdy[2]
Q4 0.14066500 ActNor.EstInrToBdy[3]
GPS sec 1231506695.000 ActNor.EstTime
MPS Cmd Vector X 0.417363000
MPS Cmd Vector Y -0.829655000
MPS Cmd Vector Z -0.370784000
MPS Diff 0.646 deg
CSS Angle TLM 1.60803
CSS Sun-Pointing Angle 3.21606
09 Jan 19 @19:00
CSS Angle TLM 0.754333
CSS Sun-Pointing Angle 1.508666
14 Jan 19 @13:00
Pre-Burn
Thruster 1 3888 09 Jan 19 @19:00
Thruster 2 3792
Thruster 3 4672
Thruster 4 4768
Post-Burn
Thruster 1 4288 14 Jan 19 @13:00
Thruster 2 4192
Thruster 3 5088
Thruster 4 5184
Number of Pulses
Thruster 1 400
Thruster 2 400
Thruster 3 416
Thruster 4 416
Thruster Pairs
Thruster 1 & 2 800
Thruster 3 & 4 832
Eric Chubin
Mission Operations Engineer - OCO2, IBEX
Northrop Grumman Innovation Systems
OCO2 MOC#: (703) 429 - 7015
Mobile#: (240) 328 - 2098
Eric.Chubin@ngc.com