All,
The perigee contacts were nominal for CMD and TLM. The Inertial maneuver was successful.
The following was completed:
CAR #1010 ATS Upload – IBEX_2018_343_o0430a_v001.scr
SSR Dump
Reset Master Timer
Set the SC Clock
Dump FC Back Orbit Data
Results from the Inertial Maneuver:
Q1 0.69344300 ActNor.EstInrToBdy[0]
Q2 0.44376900 ActNor.EstInrToBdy[1]
Q3 -0.49072400 ActNor.EstInrToBdy[2]
Q4 0.28530000 ActNor.EstInrToBdy[3]
GPS sec 1227555100.000 ActNor.EstTime
MPS Cmd Vector X -0.420876000
MPS Cmd Vector Y -0.828588000
MPS Cmd Vector Z -0.369195000
MPS Diff 0.877 deg
CSS Angle TLM 1.70949
CSS Sun-Pointing Angle 3.41898
27 Nov 18 @23:30
CSS Angle TLM 0.483355
CSS Sun-Pointing Angle 0.96671
29 Nov 18 @19:30
Pre-Burn
Thruster 1 1120 27 Nov 18 @23:30
Thruster 2 1120
Thruster 3 1200
Thruster 4 1200
Post-Burn
Thruster 1 1392 29 Nov 18 @19:30
Thruster 2 1392
Thruster 3 1504
Thruster 4 1504
Number of Pulses
Thruster 1 272
Thruster 2 272
Thruster 3 304
Thruster 4 304
Thruster Pairs
Thruster 1 & 2 544
Thruster 3 & 4 608
Eric Chubin
Mission Operations Engineer - OCO2, IBEX
Northrop Grumman Innovation Systems
OCO2 MOC#: (703) 429 - 7015
Mobile#: (240) 328 - 2098
Eric.Chubin@ngc.com