All,
The perigee contacts were nominal for CMD and TLM. The Inertial maneuver was successful.
The following was completed:
CAR 1006 ATS Upload – IBEX_2018_325_o0428a_LGC_V001
Reset Master Timer
SSR Dump and reset the pointers to 6500
Set the SC Clock
Reset FDC Totals
Results from the Inertial maneuver:
Q1 0.79563000 ActNor.EstInrToBdy[0]
Q2 -0.17275700 ActNor.EstInrToBdy[1]
Q3 -0.24091300 ActNor.EstInrToBdy[2]
Q4 0.52828900 ActNor.EstInrToBdy[3]
GPS sec
1226772670.000 ActNor.EstTime
MPS Cmd Vector X -0.559607000
MPS Cmd Vector Y -0.756679000
MPS Cmd Vector Z -0.338048000
MPS Diff
0.794 deg
CSS Angle TLM 1.35595
CSS Sun-Pointing Angle 2.7119
18 Nov 18 @ 04:30
CSS Angle TLM 1.35595
CSS Sun-Pointing Angle 2.7119
20 Nov 18 @ 18:00
Pre-Burn
Thruster 1 544 18 Nov 18 @ 04:30
Thruster 2 544
Thruster 3 592
Thruster 4 592
Post-Burn
Thruster 1 816 20 Nov 18 @ 18:00
Thruster 2 816
Thruster 3 896
Thruster 4 896
Number of Pulses
Thruster 1 272
Thruster 2 272
Thruster 3 304
Thruster 4 304
Thruster Pairs
Thruster 1 & 2 544
Thruster 3 & 4 608
Timothy E. Perry
Mission Operations
CRS, IBEX, OCO-2 & TESS
RAPTOR Test Team
Office (703) 406-5976
Cell (301) 606-1430